Philip Medlicott Ltd

Philip Medlicott Ltd

Composite Flywheel

Philip Medlicott was the inventor and designer of the composite high speed flywheel (EP 0 145 182) that ran inside the BP KESS (kinetic energy storage system) vehicle regenerative braking system, developed between 1980 and 1986.  Although the BP development is over 20 years old the technology and experience is still highly relevant. The BP KESS technology was abruptly discontinued as a consequence of the changing market conditions arising from the sudden fall in the oil price in the mid 80's which removed much of the fuel savings incentive provided by a regenerative braking system. The recent increases in fuel prices and the adoption of the regenerative breaking technology in Formula 1 has resulted in renewed interest in flywheel technology.

Design concept

The flywheel hub design provided an innovative solution to enable the high radial strain experienced by the flywheel rim to be coupled with the relatively small strain found at the shaft. The 1.44 MJ (400 Whr), 460 mm diameter, 16,000 rpm composite flywheel design was extensively modelled with FE and validated by spin testing. Other work concentrated on addressing rotor dynamics and the design of the support system to enable the flywheel to operate above the critical speed. The flywheel rotor was supported in the horizontal plane between two sets of matched ball bearings which themselves were located on squeeze film dampers. The flywheel was run inside an innovative containment system which provided a means to withstand the high temperatures and radial loads produced during the containment event.

The flywheel and containment system operated inside an outer case, which also provided a means to support the external gearbox. A rotating magnetic seal on the end of the flywheel shaft enabled the rotor to be run under vacuum to minimise aerodynamic drag. The system incorporated a microprocessor based monitoring system to detect the possible early onset of flywheel failure by monitoring vibration, vacuum, bearing temperature etc. The manufacture of the flywheel system was based on quantity production methods to enable a reasonable pay back time on the bases of savings in operating cost. A subsequent analysis of the manufacturing costs for the prototype showed that this could be achieved.

Testing

The system was subjected to several thousand hours (50,000 cycles) of endurance testing on a test rig where it was cycled between 8,000 and 16,000 rpm. In addition tests were carried out with rotors, some deliberately damaged, at speeds up to 25,800 rpm to try to initiate a catastrophic failure. In all cases the failure was initiated by a dynamic instability and resulted in a benign failure mode, i.e. the rim remained essentially intact, which was an in keeping with the system design philosophy. Finally the system was tested on a test track to demonstrate its compatibility with a bus (16 tonne) environment, for example shock loads from uneven road surfaces. These tests also included cornering tests at the maximum flywheel design speed to determine the sensitivity of the flywheel vibration characteristics to large gyroscopic forces.

Further information

  • Further information about the KESS development can be found in the following references: "Development of a Lightweight, Low Cost Flywheel Energy Storage System for a Regenerative Braking Application", PAC Medlicott, BP Research Centre, Proceedings of the 20th Intersociety Energy Conversion Engineering Conference (IECEC), Miami Beach, Florida, August 18 - 23, 1985.
  • "The Development of a Composite Flywheel Rotor for Vehicle Applications - A Study of the Interaction between Design, Materials and Fabrication", PAC Medlicott and KD Potter, BP Research Centre, High Tech - The Way into the Nineties, edited by K Brunsch et al, Elsevier Science Publishers BV, Amsterdam 1986.
    For further information and details of published papers please click contact details.

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